Wednesday, August 9, 2017

It All Started with Replacing the Arbor Bearings in my Table Saw

I have a few furniture projects coming up and I've known for a while now that the arbor bearings in my table saw needed replacing. If you've never assumed this task it's a fairly involved process that typically requires removing the weighty cast iron top. The actual job of replacing the bearings is not difficult as long as you know to use physics to your advantage. When you cool things they shrink and when you heat things they expand. I put the arbor in the freezer and when I was ready to put on the new bearings I heated them just a bit. Presto! They slide right on.

This is where things went wrong. As you know table saw dust collection is typically inadequate at best and while the top was off my saw I deemed this to be the time to design an improvement. 4 versions of a blade shroud later my saw dust collection is greatly improved. I'm into this project for way more days than I ever imagined and this spawned an entire re-arrangement of my shop. It was one of those, "while I'm at it I may as well", kind of thing.

The table saw has been moved forward and to the right approximately 2 feet. Doesn't sound like much of a task until you consider that the dust collection drop and the electrical feed also required moving. You can see evidence of the prior location in the picture below.




While the shop was in a total state of disarray I decided that now would also be the time to move my Powermatic 90 lathe to the other end of the shop. It's on a mobile base so easy right? Nope. This required me taking out the leg of my dust collection that went to the lathe, cap it off and then extend the main trunk of the system to the front end of the shop where the lathe now resides. Next I found myself crawling under my shop in order to pull a 220 volt circuit to the new lathe location while my wife was feeding the wire from inside the shop. Yes she is an extraordinary woman.




The lathe move was to facilitate moving my disc sander and oscillating spindle sander off a rolling tool chest into a fixed location on the back wall where the lathe used to reside. This required building cantilever brackets that attached to the back wall giving these tools a permanent home. I so hated having to roll that tool chest out every time I needed to use one of those tools. No more. Fortunately no electrical work was required for these machines. This sets me up to complete the finish work needed on the back wall of the shop. Trim and paint. You can see where the gray floor paint stops in the photo below. I'll be glad when the floor is all one color.





Last but not least Julie emptied out the cupboards of my Shaker workbench so we could change it's location. Even with the cupboard empty it was still quite heavy. That's part of why it's such a good workbench. We rocked it so that we could slide cardboard skids underneath. All this to move it approximately 2 feet.




Of course now the main room of the shop had the look of, "was anyone hurt when the bomb went off?"

It was time for a major aftermath clean up.


This was the final part of the re-arrangement and it all started with changing arbor bearings.

Just so you know, you can follow Brese Plane on Instagram. I'm enjoying the Instragram account. It allows me to post things going on in the shop in closer to real time and it's less involved than writing a blog post which can be hard to find the time to do.


Ron

“Whenever you find yourself on the side of the majority, it is time to pause and reflect.”
-Mark Twain

10 comments:

  1. I appreciate all you're saying brother! The bomb HAS gone off in my shop, and shrapnel is everywhere! I'm in the process off cleanup and rearranging,all while actually working as much as I can.

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  2. This is some good work! Your workshop looks much better after, i personally am very scared of table saws but you look like you have mastered the art of using and ahem cleaning them!

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